- Wed Apr 29, 2015 11:54 am
#47211
Hopefully got it sorted. When we check the crankshaft, it was about 16thou out. After a good deal of huffing and puffing and re-measuring we got it down to 2/3thou which I am happy with. I did trial fit the crankcase halves together without Wellseal first with new thrust washers to check all was ok and then pulled it apart, put the goo on and tightened it up again. Typical, I screwed the oil pump worm onto the timing pinion before inserting the timing cogs, thus obscuring the timing marks!
Thanks for all your contributions.
Dave
Thanks for all your contributions.
Dave