- Thu Nov 12, 2015 7:52 pm
#52391
Went for a spin today after fitting the bigger pilot jet. What I didn't mention last time I wrote, was that I discovered a split in the carb/tea caddy rubber connector. As a temporary fix I cut a sleeve from an old inner tube and fitted it over the torn connector. The bike started as usual today, but what surprised me was that I was able to knock off the enrichment lever almost immediately. She seemed to warm up much more quickly than before increasing the jet size, and the improvement in slow speed traffic was incredible. Now, I'm wondering if this was ALL due to the richer pilot jet, or had that rubber been split for a very long time without me noticing. If this is the case it just goes to show how important the little details are. I look forward to your valued comments.