- Mon Jul 22, 2019 7:00 am
#84271
Well looks like finally have gotten to the bottom of this problem.
Issue was a dodgy connection from fast idle cable connection to the throttle body. Was either not connected properly from PDI or may have been knocked during delivery....
Whilst in for other work this was fitted correctly and touch wood, not tempting fate the bike has now done 200 miles without a violent stall and subsequent MIL illumination. Thats with the air filter venturi fitted and aftermarket pipe also!!
The thinking from MotoGB and dealer is that by not being sealed correctly excess air is entering the throttle body and throwing ECU out....
Hopefully wont need to splash out on a PC5 or carb conversion now.....
Thanks for all the help and advice hopefully it is this simple fix....we shall see....
Issue was a dodgy connection from fast idle cable connection to the throttle body. Was either not connected properly from PDI or may have been knocked during delivery....
Whilst in for other work this was fitted correctly and touch wood, not tempting fate the bike has now done 200 miles without a violent stall and subsequent MIL illumination. Thats with the air filter venturi fitted and aftermarket pipe also!!
The thinking from MotoGB and dealer is that by not being sealed correctly excess air is entering the throttle body and throwing ECU out....
Hopefully wont need to splash out on a PC5 or carb conversion now.....
Thanks for all the help and advice hopefully it is this simple fix....we shall see....