- Mon Apr 30, 2018 10:45 pm
#76278
Lone Wolf, That's what I wanted to hear. Sounds a bit like my mate, Rick's bike. So maybe I should not worry. John T, yes I got those dimensions with the piston. Alan R, I am presuming you are the Alan from our host. Correct me if I'm wrong. But if you are, I did send you photos of the original holey piston to which you replied the obvious, too lean or too advanced which I was sure was not the problem. Someone may suggest my valve timing was out so I will beat you to it. Blind Freddy could line up those dots on the cam wheels. Ignition timing was spot on, static and full advance. Yes, it was a 200074C. I can't blame you for not replacing it, or at least giving me a pensioner's discount (joke) on another as you could presume I knew nothing about tuning and it was all my fault. However the motor was assembled and tuned by a competent RE mechanic well known to yourselves whose name I won't mention to protect the innocent. So, no I never did find out why it blew but that was two years ago. My latest operation is this new piston 90020 and I am using my standard head, standard silencer, free flowing air filter, and 125 main jet. It runs well, so well in fact I now have to attend to my slipping clutch problem and the plug looks good, a bit rich if anything. I have yet to do a plug chop at WOT but that can wait till it's run in. Beware, I may start a thread on slipping clutches next.